- Joined
- Oct 31, 2006
- Messages
- 1,394
- Points
- 1,648
ya, i was the white shirt guy. Aiyoh, y u didn't pop up ur hood? At least i can take a peek to ur engine room mah.
The actuator rod was adjusted to the max in order to avoid overboost during tuning process, hence the turbo was lag, powerband was not good before 4000rpm. Anyway, overboost was still there, it went up to 0.8 bar~
No choice, wastegate is the only solution now, and fuel pump has to be replaced also.
O ya, and the clutch slipped when VTEC kick in at 3rd gear, hahaha~~
adeh....my engine bay not nice de la...too many remix @@...no money for doing it nicely now..
yeah i already knew the turbo gona lag...
i wanted to know 1 thing..when the time u do your piping, did u told anyone how the piping's design or did anyone guide u ?
aiya boost controller kasi masuk ajer...
fuel pump is better to replace for a better one...and fuel regulator too
lol..then racing clutch lo :D...
so do u feel the different before BOT and after BOT?
and now your turbo kick-in in wat RPM range?and max boost on?
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